Part 7: Impact of Dissolved Oxygen Reduction on Nitrogen Removal Efficiency and Microbial Community in a Large-Scale Activated Sludge Process** ...

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Part 7: Impact of Dissolved Oxygen Reduction on Nitrogen Removal Efficiency and Microbial Community in a Large-Scale Activated Sludge Process** ...
Part 7: Impact of Dissolved Oxygen Reduction on Nitrogen Removal Efficiency and Microbial Community in a Large-Scale Activated Sludge Process** ๐ŸŒŠ

### **DO Control and Aeration Strategies Implemented (2011-2016)** ๐ŸŒฌ๏ธ

**Overview:**
This section summarizes the changes in dissolved oxygen (DO) control and aeration strategies at the Changi Water Reclamation Plant between January 2011 and July 2016. The study is divided into two phases:

- **Phase I:** January 2011 - March 2014
- **Phase II:** April 2014 - July 2016

**Phase I: Higher DO Concentration**
- **DO Levels:** ๐ŸŒŸ Consistently maintained at 1.7 (ยฑ0.5) mg Oโ‚‚/L.
- **Daily Air Supply:** 660,814 mยณ/day.
- **Air/Primary Effluent Ratio:** 3.4 (ยฑ0.5) mยณ/mยณ.
- **Performance:** โš™๏ธ The system operated stably with no significant changes in performance.

**Phase II: Reduced Aeration Air Supply**
- **DO Levels:** ๐Ÿ’ก Reduced to 1.0 (ยฑ0.4) mg Oโ‚‚/L.
- **Daily Air Supply:** Reduced to 605,130 mยณ/day.
- **Impacts:**
- **COD Mass Loading:** ๐Ÿ“‰ Decreased by 6%.
- **Total Nitrogen (TN) and Ammonium (NHโ‚„-N) Loading:** ๐Ÿ“ˆ Increased by 9%.
- **Conditions:** ๐ŸŒก๏ธ Temperature, pH, alkalinity, and sludge retention time (SRT) remained stable.

**Primary Cause of Changes:**
- **DO Reduction:** ๐Ÿงช The main driver of changes in process performance and microbial dynamics.

**Impact on Microbial Community and Nitrogen Removal Efficiency:**
- **Microbial Shifts:**
- **AOB (Ammonia-Oxidizing Bacteria):** ๐Ÿฆ  Decreased significantly.
- **NOB (Nitrite-Oxidizing Bacteria):** ๐Ÿ”ฌ Increased in activity.
- **Performance Impact:**
- **AOB/NOB Activity Ratio:** ๐Ÿ“‰ Decreased.
- **Nitrite Accumulation:** ๐Ÿ“‰ Reduced.
- **Anammox Activity:** ๐Ÿ“‰ Declined.
- **Nitrogen Removal Type:** ๐Ÿ”„ Shifted from autotrophic to heterotrophic.

**Overview:**
This case study examines the impact of dissolved oxygen (DO) reduction on the partial nitritation/anammox (PN/A) process and excess biological phosphorus removal at the Changi Water Reclamation Plant in Singapore. It focuses on the 200,000 mยณ/d step-feed activated sludge process (Train 2) from 2011 to 2016, evaluating process performance and microbial community dynamics.

#### **Key Findings:**

- **Dissolved Oxygen (DO) Reduction:**
- **DO Levels:** ๐Ÿ“‰ Dropped from 1.7 to 1.0 mg Oโ‚‚/L.
- **Effluent Concentrations:**
- **Ammonium and Nitrate:** ๐ŸŒŸ Increased.
- **Nitrite:** โŒ Decreased.
- **Total Inorganic Nitrogen (TIN):** ๐Ÿ“ˆ Increased by 2.4 mg N/L.

- **Nitrogen Removal Shifts:**
- **Autotrophic Removal:** ๐ŸŒฟ Higher under high DO conditions.
- **Heterotrophic Removal:** ๐Ÿ”„ Increased under low DO conditions.

- **Microbial Community Changes:**
- **Ammonia-Oxidizing Bacteria (AOB):** ๐Ÿฆ  Reduced by 30 times.
- **Nitrite-Oxidizing Bacteria (NOB):** ๐Ÿ”ฌ Increased; shift from Nitrobacter to Nitrospira.
- **AOB/NOB Activity Ratio:** ๐Ÿ“‰ Dropped from 12.8 to 1.6.
- **Nitrite Accumulation Ratio:** ๐Ÿ“‰ Reduced from 76% to 29%.
- **Anammox Bacteria Activity:** ๐Ÿ“‰ Decreased.

**Conclusion:**
The reduction in DO levels from higher to lower values resulted in significant shifts in both microbial communities and process performance. Specifically, lower DO levels decreased ammonia-oxidizing bacteria (AOB) while increasing nitrite-oxidizing bacteria (NOB), impacting nitrogen removal efficiency and microbial activity. Effective management of DO levels is essential for maintaining optimal performance and balance in activated sludge processes. ๐ŸŒŸ
DO reduction significantly impacts microbial communities and PN/A process performance, affecting nitrogen conversion and highlighting implications for biofilm and hybrid PN/A processes.

**References:**
1. Cao, Y., et al. (2018). The influence of dissolved oxygen on partial nitritation/anammox performance and microbial community at the Changi Water Reclamation Plant (2011 to 2016).

Figure 1: The volumetric ratio of air supply to primary effluent flow (m3/m3) and the DO (mg O2/L) in the aerobic zones of Train 2.

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